Fix for incorrect RPM reported.
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@ -80,7 +80,8 @@ class PWMFanUsermod : public Usermod {
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// detach interrupt while calculating rpm
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detachInterrupt(digitalPinToInterrupt(tachoPin));
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// calculate rpm
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last_rpm = counter_rpm * (60 / numberOfInterrupsInOneSingleRotation);
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last_rpm = (counter_rpm * 60) / numberOfInterrupsInOneSingleRotation;
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last_rpm /= tachoUpdateSec;
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// reset counter
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counter_rpm = 0;
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// store milliseconds when tacho was measured the last time
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